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sparse reports multiple problems with address space type.
Most problems are linked to missing __iomem qualifier.
Others are caused by dereferencing __iomem addresses.
Fix all this by adding missing __iomem and using ioread32be().
Reported-by: kernel test robot <lkp@intel.com>
Closes: https://lore.kernel.org/oe-kbuild-all/202312050412.zN2PKArS-lkp@intel.com/
Signed-off-by: Christophe Leroy <christophe.leroy@csgroup.eu>
Link: https://lore.kernel.org/r/e49deeb079391ff7273ec32f5563df94cf70bc95.1701781976.git.christophe.leroy@csgroup.eu
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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When using the serial port as RS485 port, the tx statemachine is used to
control the RTS pin to drive the RS485 transceiver TX_EN pin. When the
TTY port is closed in the middle of a transmission (for instance during
userland application crash), imx_uart_shutdown disables the interface
and disables the Transmission Complete interrupt. afer that,
imx_uart_stop_tx bails on an incomplete transmission, to be retriggered
by the TC interrupt. This interrupt is disabled and therefore the tx
statemachine never transitions out of SEND. The statemachine is in
deadlock now, and the TX_EN remains low, making the interface useless.
imx_uart_stop_tx now checks for incomplete transmission AND whether TC
interrupts are enabled before bailing to be retriggered. This makes sure
the state machine handling is reached, and is properly set to
WAIT_AFTER_SEND.
Fixes: cb1a60923609 ("serial: imx: implement rts delaying for rs485")
Signed-off-by: Paul Geurts <paul_geurts@live.nl>
Tested-by: Rasmus Villemoes <rasmus.villemoes@prevas.dk>
Tested-by: Eberhard Stoll <eberhard.stoll@gmx.de>
Link: https://lore.kernel.org/r/AM0PR09MB26758F651BC1B742EB45775995B8A@AM0PR09MB2675.eurprd09.prod.outlook.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Granite Rapids-D has an additional UART that is enumerated via ACPI.
Add ACPI ID for it.
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Cc: stable <stable@kernel.org>
Link: https://lore.kernel.org/r/20231205195524.2705965-1-andriy.shevchenko@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The console is immediately assigned to the ma35d1 port without
checking its index. This oversight can lead to out-of-bounds
errors when the index falls outside the valid '0' to
MA35_UART_NR range. Such scenario trigges ran error like the
following:
UBSAN: array-index-out-of-bounds in drivers/tty/serial/ma35d1_serial.c:555:51
index -1 is out of range for type 'uart_ma35d1_port [17]
Check the index before using it and bail out with a warning.
Fixes: 930cbf92db01 ("tty: serial: Add Nuvoton ma35d1 serial driver support")
Signed-off-by: Andi Shyti <andi.shyti@kernel.org>
Cc: Jacky Huang <ychuang3@nuvoton.com>
Cc: <stable@vger.kernel.org> # v6.5+
Link: https://lore.kernel.org/r/20231204163804.1331415-2-andi.shyti@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Designware UART has an optional feature to enable Fractional Baud Rate
Divisor (DLF) through the FRACTIONAL_BAUD_DIVISOR_EN configuration
parameter, and it is not dependent on ADDITIONAL_FEATURES.
dw8250_setup_port() checks DLF to determine dlf_size only when UART
Component Version (UCV) is non-zero. As mentioned above DLF and UCV are
independent features. Move the logic corresponding to DLF size
calculation ahead of the UCV check to prevent early return. Otherwise,
dlf_size will be zero and driver will not be able to use the
controller's fractional baud rate divisor (DLF) feature.
Signed-off-by: Vamshi Gajjela <vamshigajjela@google.com>
Link: https://lore.kernel.org/r/20231126160420.2442330-1-vamshigajjela@google.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The comment wording can be confusing, as txlen will return the number of
bytes available in the FIFO, which can be less than the maximum theoretical
Tx FIFO size.
Change the comment so that it is unambiguous.
Signed-off-by: Hugo Villeneuve <hvilleneuve@dimonoff.com>
Link: https://lore.kernel.org/r/20231122175957.3875102-1-hugo@hugovil.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The comment wording can be confusing, as txlen will return the number of
bytes available in the FIFO, which can be less than the maximum theoretical
Tx FIFO size.
Change the comment so that it is unambiguous.
Signed-off-by: Hugo Villeneuve <hvilleneuve@dimonoff.com>
Link: https://lore.kernel.org/r/20231122175859.3874753-1-hugo@hugovil.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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This reverts commit 81a61051e0ce5fd7e09225c0d5985da08c7954a7.
With tty and serdev controller moved to be children of the serial core
port device, runtime PM usage count of the serdev controller now
propagates to the serial hardware controller parent device as expected.
Cc: Maximilian Luz <luzmaximilian@gmail.com>
Cc: Rob Herring <robh@kernel.org>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Reviewed-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Link: https://lore.kernel.org/r/20231113080758.30346-2-tony@atomide.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Let's move tty and serdev controller to be children of the serial core port
device. This way the runtime PM usage count of a child device propagates
to the serial hardware device.
The tty and serdev devices are associated with a specific serial port of
a serial hardware controller device, and we now have serial core hierarchy
of controllers and ports.
The tty device moves happily with just a change of the parent device and
update of device_find_child() handling. The serdev device init needs some
changes to separate the serial hardware controller device from the parent
device.
With this change the tty devices move under sysfs similar to this x86_64
qemu example of a diff of "find /sys -name ttyS*":
/sys/class/tty/ttyS0
/sys/class/tty/ttyS3
/sys/class/tty/ttyS1
-/sys/devices/pnp0/00:04/tty/ttyS0
-/sys/devices/platform/serial8250/tty/ttyS2
-/sys/devices/platform/serial8250/tty/ttyS3
-/sys/devices/platform/serial8250/tty/ttyS1
+/sys/devices/pnp0/00:04/00:04:0/00:04:0.0/tty/ttyS0
+/sys/devices/platform/serial8250/serial8250:0/serial8250:0.3/tty/ttyS3
+/sys/devices/platform/serial8250/serial8250:0/serial8250:0.1/tty/ttyS1
+/sys/devices/platform/serial8250/serial8250:0/serial8250:0.2/tty/ttyS2
If a serdev device is used instead of a tty, it moves in a similar way.
Suggested-by: Johan Hovold <johan@kernel.org>
Cc: Maximilian Luz <luzmaximilian@gmail.com>
Cc: Rob Herring <robh@kernel.org>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Link: https://lore.kernel.org/r/20231113080758.30346-1-tony@atomide.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Device number 204 has a range of minors on major number.
uart_register_driver is failing due to lack of minor numbers
when more number of uart ports used. So, to avoid minor number
limitation on 204 major number use dynamic major allocation
when more than 4 uart ports used otherwise use static major
allocation.
https://docs.kernel.org/arch/arm/sa1100/serial_uart.html
Signed-off-by: Manikanta Guntupalli <manikanta.guntupalli@amd.com>
Link: https://lore.kernel.org/r/20231116134003.3762725-3-manikanta.guntupalli@amd.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Since the driver was converted to use .remove_new() the return function
doesn't return a value any more. So remove the obsolete documentation
about the return value.
Reported-by: Michal Simek <michal.simek@amd.com>
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Michal Simek <michal.simek@amd.com>
Link: https://lore.kernel.org/r/20231117101236.878008-1-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Since there is no guarantee that the memory returned by
dma_alloc_coherent() is associated with a 'struct page', using the
architecture specific phys_to_page() is wrong, but using
virt_to_page() would be as well.
Stop using sg lists altogether and just use the *_single() functions
instead. This also simplifies the code a bit since the scatterlists in
this driver always have only one entry anyway.
https://lore.kernel.org/lkml/86db0fe5-930d-4cbb-bd7d-03367da38951@app.fastmail.com/
Use consistent names for dma buffers
gc: Add a commit log from the initial thread:
https://lore.kernel.org/lkml/86db0fe5-930d-4cbb-bd7d-03367da38951@app.fastmail.com/
Use consistent names for dma buffers
Fixes: cb06ff102e2d7 ("ARM: PL011: Add support for Rx DMA buffer polling.")
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Tested-by: Gregory CLEMENT <gregory.clement@bootlin.com>
Signed-off-by: Gregory CLEMENT <gregory.clement@bootlin.com>
Cc: stable <stable@kernel.org>
Link: https://lore.kernel.org/r/20231122171503.235649-1-gregory.clement@bootlin.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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This device has a silicon bug that makes it report a timeout interrupt
but no data in the FIFO.
The datasheet states the following in the errata section 18.1.4:
"If the host reads the receive FIFO at the same time as a
time-out interrupt condition happens, the host might read 0xCC
(time-out) in the Interrupt Indication Register (IIR), but bit 0
of the Line Status Register (LSR) is not set (means there is no
data in the receive FIFO)."
The errata description seems to indicate it concerns only polled mode of
operation when reading bit 0 of the LSR register. However, tests have
shown and NXP has confirmed that the RXLVL register also yields 0 when
the bug is triggered, and hence the IRQ driven implementation in this
driver is equally affected.
This bug has hit us on production units and when it does, sc16is7xx_irq()
would spin forever because sc16is7xx_port_irq() keeps seeing an
interrupt in the IIR register that is not cleared because the driver
does not call into sc16is7xx_handle_rx() unless the RXLVL register
reports at least one byte in the FIFO.
Fix this by always reading one byte from the FIFO when this condition
is detected in order to clear the interrupt. This approach was
confirmed to be correct by NXP through their support channels.
Tested by: Hugo Villeneuve <hvilleneuve@dimonoff.com>
Signed-off-by: Daniel Mack <daniel@zonque.org>
Co-Developed-by: Maxim Popov <maxim.snafu@gmail.com>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20231123072818.1394539-1-daniel@zonque.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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This fixes commit 439c7183e5b9 ("serial: 8250: 8250_omap: Disable RX
interrupt after DMA enable") which unfortunately set the
UART_HAS_RHR_IT_DIS bit in the UART_OMAP_IER2 register and never
cleared it.
Cc: stable@vger.kernel.org
Fixes: 439c7183e5b9 ("serial: 8250: 8250_omap: Disable RX interrupt after DMA enable")
Signed-off-by: Ronald Wahl <ronald.wahl@raritan.com>
Reviewed-by: Vignesh Raghavendra <vigneshr@ti.com>
Link: https://lore.kernel.org/r/20231031110909.11695-1-rwahl@gmx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Currently there is no support for earlycon on the AM654 UART
controller. This commit adds it.
Signed-off-by: Ronald Wahl <ronald.wahl@raritan.com>
Reviewed-by: Vignesh Raghavendra <vigneshr@ti.com>
Link: https://lore.kernel.org/r/20231031131242.15516-1-rwahl@gmx.de
Cc: stable <stable@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Starting RX DMA on THRI interrupt is too early because TX may not have
finished yet.
This change is inspired by commit 90b8596ac460 ("serial: 8250: Prevent
starting up DMA Rx on THRI interrupt") and fixes DMA issues I had with
an AM62 SoC that is using the 8250 OMAP variant.
Cc: stable@vger.kernel.org
Fixes: c26389f998a8 ("serial: 8250: 8250_omap: Add DMA support for UARTs on K3 SoCs")
Signed-off-by: Ronald Wahl <ronald.wahl@raritan.com>
Reviewed-by: Vignesh Raghavendra <vigneshr@ti.com>
Link: https://lore.kernel.org/r/20231101171431.16495-1-rwahl@gmx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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dma_request_slave_channel() is deprecated. dma_request_chan() should
be used directly instead.
Switch to the preferred function and update the error handling accordingly.
Signed-off-by: Christophe JAILLET <christophe.jaillet@wanadoo.fr>
Link: https://lore.kernel.org/r/d6773b9bd88dbbbea06bc6d5cd59aa117b1ee2ee.1700416841.git.christophe.jaillet@wanadoo.fr
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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dma_request_slave_channel() is deprecated. dma_request_chan() should
be used directly instead.
Switch to the preferred function and update the error handling accordingly.
Signed-off-by: Christophe JAILLET <christophe.jaillet@wanadoo.fr>
Link: https://lore.kernel.org/r/94812f7063e4db5590254ec45fe9bb3c6569509e.1700410918.git.christophe.jaillet@wanadoo.fr
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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dma_request_slave_channel() is deprecated. dma_request_chan() should
be used directly instead.
Switch to the preferred function and update the error handling accordingly.
Signed-off-by: Christophe JAILLET <christophe.jaillet@wanadoo.fr>
Link: https://lore.kernel.org/r/6f76e22f77d776d6c1f176d56e7ee341314d8554.1700405529.git.christophe.jaillet@wanadoo.fr
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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dma_request_slave_channel() is deprecated. dma_request_chan() should
be used directly instead.
Switch to the preferred function and update the error handling accordingly.
Signed-off-by: Christophe JAILLET <christophe.jaillet@wanadoo.fr>
Link: https://lore.kernel.org/r/a46b493c6b5cfa09417e3e138e304fd01b61e748.1700410346.git.christophe.jaillet@wanadoo.fr
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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dma_request_slave_channel() is deprecated. dma_request_chan() should
be used directly instead.
Switch to the preferred function and update the error handling accordingly.
Signed-off-by: Christophe JAILLET <christophe.jaillet@wanadoo.fr>
Link: https://lore.kernel.org/r/f2e9790d8b49aeba8b43ce018d30a35b837ac1eb.1700409299.git.christophe.jaillet@wanadoo.fr
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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With this current driver regmap implementation, it is hard to make sense
of the register addresses displayed using the regmap debugfs interface,
because they do not correspond to the actual register addresses documented
in the datasheet. For example, register 1 is displayed as registers 04 thru
07:
$ cat /sys/kernel/debug/regmap/spi0.0/registers
04: 10 -> Port 0, register offset 1
05: 10 -> Port 1, register offset 1
06: 00 -> Port 2, register offset 1 -> invalid
07: 00 -> port 3, register offset 1 -> invalid
...
The reason is that bits 0 and 1 of the register address correspond to the
channel (port) bits, so the register address itself starts at bit 2, and we
must 'mentally' shift each register address by 2 bits to get its real
address/offset.
Also, only channels 0 and 1 are supported by the chip, so channel mask
combinations of 10b and 11b are invalid, and the display of these
registers is useless.
This patch adds a separate regmap configuration for each port, similar to
what is done in the max310x driver, so that register addresses displayed
match the register addresses in the chip datasheet. Also, each port now has
its own debugfs entry.
Example with new regmap implementation:
$ cat /sys/kernel/debug/regmap/spi0.0-port0/registers
1: 10
2: 01
3: 00
...
$ cat /sys/kernel/debug/regmap/spi0.0-port1/registers
1: 10
2: 01
3: 00
As an added bonus, this also simplifies some operations (read/write/modify)
because it is no longer necessary to manually shift register addresses.
Signed-off-by: Hugo Villeneuve <hvilleneuve@dimonoff.com>
Link: https://lore.kernel.org/r/20231030211447.974779-1-hugo@hugovil.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Fix coding style. No functional changes.
Signed-off-by: Hugo Villeneuve <hvilleneuve@dimonoff.com>
Link: https://lore.kernel.org/r/20231030212240.975885-1-hugo@hugovil.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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They are only used within this file, so they should have static linkage.
Signed-off-by: Samuel Holland <samuel.holland@sifive.com>
Link: https://lore.kernel.org/r/20231113023122.1185407-1-samuel.holland@sifive.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Use @ and - to conform with kernel-doc style.
Reported-by: kernel test robot <yujie.liu@intel.com>
Signed-off-by: Sean Anderson <sean.anderson@seco.com>
Reviewed-by: Randy Dunlap <rdunlap@infradead.org>
Reviewed-by: Shubhrajyoti Datta <shubhrajyoti.datta@amd.com>
Link: https://lore.kernel.org/r/20231106152428.3641883-1-sean.anderson@seco.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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clang-struct [1] found struct serial_cfg_mem's members unused.
In fact, the whole structure is unused since commit 6ae3b84d9793
("serial_cs: use pcmcia_loop_config() and pre-determined values"). Drop
it completely.
[1] https://github.com/jirislaby/clang-struct
Signed-off-by: "Jiri Slaby (SUSE)" <jirislaby@kernel.org>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20231121103626.17772-7-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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clang-struct [1] found rp2_uart_port::ignore_rx unused.
It was actually never used. Not even in introductory commit 7d9f49afa451
("serial: rp2: New driver for Comtrol RocketPort 2 cards").
[1] https://github.com/jirislaby/clang-struct
Signed-off-by: "Jiri Slaby (SUSE)" <jirislaby@kernel.org>
Cc: Kevin Cernekee <cernekee@gmail.com>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20231121103626.17772-6-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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clang-struct [1] found jsm_board::type and ::jsm_board_entry unused.
::jsm_board_entry is unused since 614a7d6a76b7 ("fix up newly added jsm driver")
::type was never used as far as I can tell. Even when the driver was
introduced in the pre-git era.
Remove them both.
[1] https://github.com/jirislaby/clang-struct
Signed-off-by: "Jiri Slaby (SUSE)" <jirislaby@kernel.org>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20231121103626.17772-5-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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clang-struct [1] found board_ops::get_uart_bytes_left() and
::send_immediate_char() unused.
Both are only set but never called. And it has been like that since the
git history, so drop both the members along with the cls+neo
implementations.
[1] https://github.com/jirislaby/clang-struct
Signed-off-by: "Jiri Slaby (SUSE)" <jirislaby@kernel.org>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20231121103626.17772-4-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-53-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-52-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-51-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-50-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-49-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-48-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-47-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-46-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-45-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-44-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-43-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-42-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Chunyan Zhang <zhang.lyra@gmail.com>
Link: https://lore.kernel.org/r/20231110152927.70601-41-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Reviewed-by: Samuel Holland <samuel.holland@sifive.com>
Link: https://lore.kernel.org/r/20231110152927.70601-40-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Reviewed-by: Geert Uytterhoeven <geert+renesas@glider.be>
Link: https://lore.kernel.org/r/20231110152927.70601-39-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-38-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-37-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-36-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Reviewed-by: Krzysztof Kozlowski <krzysztof.kozlowski@linaro.org>
Link: https://lore.kernel.org/r/20231110152927.70601-35-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-34-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|
|
The .remove() callback for a platform driver returns an int which makes
many driver authors wrongly assume it's possible to do error handling by
returning an error code. However the value returned is ignored (apart
from emitting a warning) and this typically results in resource leaks.
To improve here there is a quest to make the remove callback return
void. In the first step of this quest all drivers are converted to
.remove_new(), which already returns void. Eventually after all drivers
are converted, .remove_new() will be renamed to .remove().
Trivially convert this driver from always returning zero in the remove
callback to the void returning variant.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20231110152927.70601-33-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
|