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The commit 646cafc6 (clk: Change clk_ops->determine_rate to
return a clk_hw as the best parent) opens a possibility for
null pointer dereference, fix this.
Signed-off-by: Stanimir Varbanov <svarbanov@mm-sol.com>
Reviewed-by: Stephen Boyd <sboyd@codeaurora.org>
Signed-off-by: Michael Turquette <mturquette@linaro.org>
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This reverts commit da788acb28386aa896224e784954bb73c99ff26c.
That commit tried to fix the section mismatch warning by moving the
ppc_corenet_clk_driver struct to init section. This is definitely wrong
because the kernel would free the memories occupied by this struct
after boot while this driver is still registered in the driver core.
The kernel would panic when accessing this driver struct.
Cc: stable@vger.kernel.org # 3.17
Signed-off-by: Kevin Hao <haokexin@gmail.com>
Acked-by: Scott Wood <scottwood@freescale.com>
Signed-off-by: Michael Turquette <mturquette@linaro.org>
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Lockdep reported a possible deadlock between the cpuclk lock and for example
the i2c driver.
CPU0 CPU1
---- ----
lock(clk_lock);
local_irq_disable();
lock(&(&i2c->lock)->rlock);
lock(clk_lock);
<Interrupt>
lock(&(&i2c->lock)->rlock);
*** DEADLOCK ***
The generic clock-types of the core ccf already use spin_lock_irqsave when
touching clock registers, so do the same for the cpuclk.
Signed-off-by: Heiko Stuebner <heiko@sntech.de>
Reviewed-by: Doug Anderson <dianders@chromium.org>
Signed-off-by: Michael Turquette <mturquette@linaro.org>
[mturquette@linaro.org: removed initialization of "flags"]
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Pull dmaengine fixes from Vinod Koul:
"Two patches, the first by Andy to fix dw dmac runtime pm and second
one by me to fix the dmaengine headers in MAINTAINERS"
* 'fixes' of git://git.infradead.org/users/vkoul/slave-dma:
dmaengine: dw: balance PM runtime calls
MAINTAINERS: dmaengine: fix the header file for dmaengine
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Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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Instead of pushing each byte via stack the specifier allows to supply the
pointer and length to dump buffers up to 64 bytes long.
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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This is an important optimization for avoiding read-after-write (RAW)
stalls in the HiZ buffer. Certain workloads would run very slowly with
HiZ enabled, but run much faster with the "hiz=false" driconf option.
With this patch, they run at full speed even with HiZ.
Increases performance in OglVSInstancing by about 2.7x on Braswell.
Signed-off-by: Kenneth Graunke <kenneth@whitecape.org>
Reviewed-by: Ville Syrjälä <ville.syrjala@linux.intel.com>
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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This is an important optimization for avoiding read-after-write (RAW)
stalls in the HiZ buffer. Certain workloads would run very slowly with
HiZ enabled, but run much faster with the "hiz=false" driconf option.
With this patch, they run at full speed even with HiZ.
Improves performance in OglVSInstancing by 3.2x on Broadwell GT3e
(Iris Pro 6200).
Thanks to Jesse Barnes and Ben Widawsky for their help in tracking this
down. Thanks to Chris Wilson for showing me the new workarounds system.
Signed-off-by: Kenneth Graunke <kenneth@whitecape.org>
Cc: Jesse Barnes <jbarnes@virtuousgeek.org>
Reviewed-by: Ville Syrjälä <ville.syrjala@linux.intel.com>
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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Call spin_lock_init() before the spinlocks are used, both in early init
and probe functions preventing a lockdep splat.
I have been observing lockdep complaining [1] during boot on my a80 optimus [2]
when CONFIG_PROVE_LOCKING has been enabled. This patch resolves the splat,
and has been tested on a few other sunxi platforms without issue.
[1] http://storage.kernelci.org/next/next-20150107/arm-multi_v7_defconfig+CONFIG_PROVE_LOCKING=y/lab-tbaker/boot-sun9i-a80-optimus.html
[2] http://kernelci.org/boot/?a80-optimus
Signed-off-by: Tyler Baker <tyler.baker@linaro.org>
Cc: <stable@vger.kernel.org>
Acked-by: Philipp Zabel <p.zabel@pengutronix.de>
Signed-off-by: Kevin Hilman <khilman@linaro.org>
Signed-off-by: Olof Johansson <olof@lixom.net>
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The arm-cci driver completes the probe sequence even if the cci node is
marked as disabled. Add a check in the driver to honour the cci status
in the device tree.
Signed-off-by: Abhilash Kesavan <a.kesavan@samsung.com>
Acked-by: Sudeep Holla <sudeep.holla@arm.com>
Acked-by: Nicolas Pitre <nico@linaro.org>
Tested-by: Sudeep Holla <sudeep.holla@arm.com>
Tested-by: Kevin Hilman <khilman@linaro.org>
Signed-off-by: Olof Johansson <olof@lixom.net>
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git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/char-misc
Pull char/misc driver fixes from Greg KH:
"Here are three small driver fixes for reported issues for 3.19-rc5.
All of these have been in linux-next for a while with no reported
problems"
* tag 'char-misc-3.19-rc5' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/char-misc:
mcb: mcb-pci: Only remap the 1st 0x200 bytes of BAR 0
mei: add ABI documentation for fw_status exported through sysfs
mei: clean reset bit before reset
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git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty
Pull tty/serial driver fixes from Greg KH:
"Here are some tty and serial driver fixes for 3.19-rc5 that resolve
some reported issues, and add a new device id to the 8250 serial port
driver.
All have been in linux-next with no reported problems"
* tag 'tty-3.19-rc5' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty:
serial: samsung: Add the support for Exynos5433 SoC
Revert "tty: Fix pty master poll() after slave closes v2"
tty: Prevent hw state corruption in exclusive mode reopen
tty: Add support for the WCH384 4S multi-IO card
serial: fix parisc boot hang
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git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/staging
Pull staging driver fixes from Greg KH:
"Here are 6 staging driver fixes for 3.19-rc5.
They fix some reported issues with some IIO drivers, as well as some
issues with the vt6655 wireless driver.
All have been in linux-next for a while"
* tag 'staging-3.19-rc5' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/staging:
staging: vt6655: fix sparse warning: argument type
staging: vt6655: Fix loss of distant/weak access points on channel change.
staging: vt6655: vnt_tx_packet Fix corrupted tx packets.
staging: vt6655: fix sparse warnings: incorrect argument type
iio: iio: Fix iio_channel_read return if channel havn't info
iio: ad799x: Fix ad7991/ad7995/ad7999 config setup
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git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/usb
Pull USB fixes from Greg KH:
"Here is a bunch of USB fixes for 3.19-rc5.
Most of these are gadget driver fixes, along with the xhci driver fix
that we both reported having problems with, as well as some new device
ids and other tiny fixes.
All have been in linux-next with no problems"
* tag 'usb-3.19-rc5' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/usb: (43 commits)
usb: dwc3: gadget: Stop TRB preparation after limit is reached
usb: dwc3: gadget: Fix TRB preparation during SG
usb: phy: mv-usb: fix usb_phy build errors
usb: serial: handle -ENODEV quietly in generic_submit_read_urb
usb: serial: silence all non-critical read errors
USB: console: fix potential use after free
USB: console: fix uninitialised ldisc semaphore
usb: gadget: udc: atmel: fix possible oops when unloading module
usb: gadget: gadgetfs: fix an oops in ep_write()
usb: phy: Fix deferred probing
OHCI: add a quirk for ULi M5237 blocking on reset
uas: Add US_FL_NO_ATA_1X for 2 more Seagate disk enclosures
uas: Do not blacklist ASM1153 disk enclosures
usb: gadget: udc: avoid dereference before NULL check in ep_queue
usb: host: ehci-tegra: request deferred probe when failing to get phy
uas: disable UAS on Apricorn SATA dongles
uas: Add US_FL_NO_REPORT_OPCODES for JMicron JMS566 with usb-id 0bc2:a013
uas: Add US_FL_NO_ATA_1X for Seagate devices with usb-id 0bc2:a013
xhci: Add broken-streams quirk for Fresco Logic FL1000G xhci controllers
USB: EHCI: adjust error return code
...
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On dm816x we have two emac controllers with separate memory
areas.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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space
Some devices like dm816x have the MDIO registers within the first EMAC
instance address space. Let's fix the issue by allowing to pass an
optional second IO range for the EMAC control register area.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Looks like the phy_id is never set up beyond getting the phandle.
Note that we can remove the ifdef for phy_node as there is a stub
for of_phy_connec() if CONFIG_OF is not set.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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We only use clk_get() to get the frequency, the rest is done by
the runtime PM calls. Let's free the clock too.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Commit 3ba97381343b ("net: ethernet: davinci_emac: add pm_runtime support")
added support for runtime PM, but it causes issues on omap3 related devices
that actually gate the clocks:
Unhandled fault: external abort on non-linefetch (0x1008)
...
[<c04160f0>] (emac_dev_getnetstats) from [<c04d6a3c>] (dev_get_stats+0x78/0xc8)
[<c04d6a3c>] (dev_get_stats) from [<c04e9ccc>] (rtnl_fill_ifinfo+0x3b8/0x938)
[<c04e9ccc>] (rtnl_fill_ifinfo) from [<c04eade4>] (rtmsg_ifinfo+0x68/0xd8)
[<c04eade4>] (rtmsg_ifinfo) from [<c04dd35c>] (register_netdevice+0x3a0/0x4ec)
[<c04dd35c>] (register_netdevice) from [<c04dd4bc>] (register_netdev+0x14/0x24)
[<c04dd4bc>] (register_netdev) from [<c041755c>] (davinci_emac_probe+0x408/0x5c8)
[<c041755c>] (davinci_emac_probe) from [<c0396d78>] (platform_drv_probe+0x48/0xa4)
Let's fix it by moving the pm_runtime_get() call earlier, and also add it to
the emac_dev_getnetstats(). Also note that we want to use pm_runtime_get_sync()
as we don't want to have deferred_resume happen. And let's also check the
return value for pm_runtime_get_sync() as noted by Felipe Balbi <balbi@ti.com>.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Acked-by: Mark A. Greer <mgreer@animalcreek.com>
Reviewed-by: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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On davinci_emac, we have pulse interrupts. This means that we need to
clear the EOI bits when disabling interrupts as otherwise the interrupts
keep happening. And we also need to not clear the EOI bits again when
enabling the interrupts as otherwise we will get tons of:
unexpected IRQ trap at vector 00
These errors almost certainly mean that the omap-intc.c is signaling
a spurious interrupt with the reserved irq 127 as we've seen earlier
on omap3.
Let's fix the issue by clearing the EOI bits when disabling the
interrupts. Let's also keep the comment for "Rx Threshold and Misc
interrupts are not enabled" for both enable and disable so people
are aware of this when potentially adding more support.
Note that eventually we should handle the RX and TX interrupts
separately like cpsw is now doing. However, so far I have not seen
any issues with this based on my testing, so it seems to behave a
little different compared to the cpsw that had a similar issue.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Reviewed-by: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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git://git.kernel.org/pub/scm/linux/kernel/git/tomba/linux
Pull fbdev fixes from Tomi Valkeinen:
- broadsheetfb: fix memory leak
- simplefb: fix build failure on sparc
* tag 'fbdev-fixes-3.19' of git://git.kernel.org/pub/scm/linux/kernel/git/tomba/linux:
fbdev/broadsheetfb: fix memory leak
simplefb: Fix build failure on Sparc
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Pull MMC bugfix from Ulf Hansson:
"Fix sdhci regulator regression for Qualcomm and Nvidia boards"
* tag 'mmc-v3.19-4' of git://git.linaro.org/people/ulf.hansson/mmc:
mmc: sdhci: Set SDHCI_POWER_ON with external vmmc
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git://git.kernel.org/pub/scm/linux/kernel/git/mpe/linux
Pull powerpc fixes from Michael Ellerman:
"A few powerpc fixes"
* tag 'powerpc-3.19-4' of git://git.kernel.org/pub/scm/linux/kernel/git/mpe/linux:
powerpc: Work around gcc bug in current_thread_info()
cxl: Fix issues when unmapping contexts
powernv: Fix OPAL tracepoint code
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git://git.kernel.org/pub/scm/linux/kernel/git/mkl/linux-can
Marc Kleine-Budde says:
====================
pull-request: can 2015-01-15
this is a pull request of 8 patches.
Ahmed S. Darwish contributes 4 fixes for the kvaser_usb driver. The two patches
by Oliver Hartkopp mark the m_can driver as non-ISO, as the CANFD standard was
updated. Roger Quadros's patch for the c_can driver fixes the register access
during RAMINIT. And one patch by my, which updates the MAINTAINERS file, as we
moved the git repos to the kernel.org infrastructure.
====================
Signed-off-by: David S. Miller <davem@davemloft.net>
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Except for VXLAN steering rules, all offloads should work as they were
under plain DMFS mode. Fix that by enabling all the offloads under
DMFS-A0 mode, except for VXLAN steering rules.
Fixes: d57febe1a478 "net/mlx4: Add A0 hybrid steering"
Signed-off-by: Or Gerlitz <ogerlitz@mellanox.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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This patch fixes double kfree() calls at init_rx_ring() because
it causes static checker warning.
Reported-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: Byungho An <bh74.an@samsung.com>
Signed-off-by: Kukjin Kim <kgene@kernel.org>
Signed-off-by: David S. Miller <davem@davemloft.net>
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When the MAC address is provided in the device tree file, the
condition is true and kernel crashes due to NULL dereference.
Signed-off-by: Girish K.S <ks.giri@samsung.com>
Signed-off-by: Byungho An <bh74.an@samsung.com>
Signed-off-by: Kukjin Kim <kgene@kernel.org>
Signed-off-by: David S. Miller <davem@davemloft.net>
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commit b284fbe3b3ef9cf8 ("sh_eth: Fix access to TRSCER register") wanted
to add a .trscer_err_mask value to the R-Car Gen2 family-specific data
structure (r8a779x_data), but it was accidentally added to the
SH7724-specific data structure (sh7724_data).
Presumably this happened due to a patch conflict with commit
d407bc0203539031 ("sh-eth: Set fdr_value of R-Car SoCs"), which added
another field at the same position.
Move the field setting to fix this.
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Fixes: b284fbe3b3ef9cf8 ("sh_eth: Fix access to TRSCER register")
Signed-off-by: David S. Miller <davem@davemloft.net>
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while adding vlan in dual EMAC mode, only specific ports should be
subscribed for the vlan, else it will lead to switching mode and
if both ports connected to same switch cpsw will hung as it creates
a network loop. Fixing this by adding only specific ports in case
of dual EMAC.
Signed-off-by: Mugunthan V N <mugunthanvnm@ti.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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of_get_named_gpiod_flags fails with -EPROBE_DEFER in cases
where the gpio chip is available and the GPIO translation fails.
This causes drivers to be re-probed erroneusly, and hides the
real problem(i.e. the GPIO number being out of range).
Cc: Stable <stable@vger.kernel.org>
Signed-off-by: Hans Holmberg <hans.holmberg@intel.com>
Reviewed-by: Alexandre Courbot <acourbot@nvidia.com>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
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Fix attribute-creation race with userspace by using the default group
to create also the contingent gpio device attributes.
Fixes: d8f388d8dc8d ("gpio: sysfs interface")
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
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The gpio device attributes were never destroyed when the gpio was
unexported (or on export failures).
Use device_create_with_groups() to create the default device attributes
of the gpio class device. Note that this also fixes the
attribute-creation race with userspace for these attributes.
Remove contingent attributes in export error path and on unexport.
Fixes: d8f388d8dc8d ("gpio: sysfs interface")
Cc: stable <stable@vger.kernel.org> # v2.6.27+
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
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The gpio-chip device attributes were never destroyed when the device was
removed.
Fix by using device_create_with_groups() to create the device attributes
of the chip class device.
Note that this also fixes the attribute-creation race with userspace.
Fixes: d8f388d8dc8d ("gpio: sysfs interface")
Cc: stable <stable@vger.kernel.org> # v2.6.27+
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
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This was accidently lost in 76a0df859def.
Signed-off-by: Alex Deucher <alexander.deucher@amd.com>
Cc: stable@vger.kernel.org
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We should not touch the packet after a netif_rx: it might
get freed behind our back.
Suggested-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
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Recent Leaf firmware versions (>= 3.1.557) do not allow to send
commands for non-existing channels. If a command is sent for a
non-existing channel, the firmware crashes.
Reported-by: Christopher Storah <Christopher.Storah@invetech.com.au>
Signed-off-by: Olivier Sobrie <olivier@sobrie.be>
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
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Flooding the Kvaser CAN to USB dongle with multiple reads and
writes in very high frequency (*), closing the CAN channel while
all the transmissions are on (#), opening the device again (@),
then sending a small number of packets would make the driver
enter an almost infinite loop of:
[....]
[15959.853988] kvaser_usb 4-3:1.0 can0: cannot find free context
[15959.853990] kvaser_usb 4-3:1.0 can0: cannot find free context
[15959.853991] kvaser_usb 4-3:1.0 can0: cannot find free context
[15959.853993] kvaser_usb 4-3:1.0 can0: cannot find free context
[15959.853994] kvaser_usb 4-3:1.0 can0: cannot find free context
[15959.853995] kvaser_usb 4-3:1.0 can0: cannot find free context
[....]
_dragging the whole system down_ in the process due to the
excessive logging output.
Initially, this has caused random panics in the kernel due to a
buggy error recovery path. That got fixed in an earlier commit.(%)
This patch aims at solving the root cause. -->
16 tx URBs and contexts are allocated per CAN channel per USB
device. Such URBs are protected by:
a) A simple atomic counter, up to a value of MAX_TX_URBS (16)
b) A flag in each URB context, stating if it's free
c) The fact that ndo_start_xmit calls are themselves protected
by the networking layers higher above
After grabbing one of the tx URBs, if the driver noticed that all
of them are now taken, it stops the netif transmission queue.
Such queue is worken up again only if an acknowedgment was received
from the firmware on one of our earlier-sent frames.
Meanwhile, upon channel close (#), the driver sends a CMD_STOP_CHIP
to the firmware, effectively closing all further communication. In
the high traffic case, the atomic counter remains at MAX_TX_URBS,
and all the URB contexts remain marked as active. While opening
the channel again (@), it cannot send any further frames since no
more free tx URB contexts are available.
Reset all tx URB contexts upon CAN channel close.
(*) 50 parallel instances of `cangen0 -g 0 -ix`
(#) `ifconfig can0 down`
(@) `ifconfig can0 up`
(%) "can: kvaser_usb: Don't free packets when tight on URBs"
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
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Flooding the Kvaser CAN to USB dongle with multiple reads and
writes in high frequency caused seemingly-random panics in the
kernel.
On further inspection, it seems the driver erroneously freed the
to-be-transmitted packet upon getting tight on URBs and returning
NETDEV_TX_BUSY, leading to invalid memory writes and double frees
at a later point in time.
Note:
Finding no more URBs/transmit-contexts and returning NETDEV_TX_BUSY
is a driver bug in and out of itself: it means that our start/stop
queue flow control is broken.
This patch only fixes the (buggy) error handling code; the root
cause shall be fixed in a later commit.
Acked-by: Olivier Sobrie <olivier@sobrie.be>
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
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use of regmap_read() and regmap_write() in c_can_hw_raminit_syscon()
is not safe as the RAMINIT register can be shared between different drivers
at least for TI SoCs.
To make the modification atomic we switch to using regmap_update_bits().
regmap_update_bits() skips writing to the register if it's read content is the
same as what is going to be written. This causes an issue for us when we
need to clear the DONE bit with the initial condition START:0, DONE:1 as
DONE bit must be written with 1 to clear it.
So we defer the clearing of DONE bit to later when we set the START bit.
There we are sure that START bit is changed from 0 to 1 so the write of
1 to already set DONE bit will happen.
Signed-off-by: Roger Quadros <rogerq@ti.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
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During the CAN FD standardization process within the ISO it turned out that
the failure detection capability has to be improved.
The CAN in Automation organization (CiA) defined the already implemented CAN
FD controllers as 'non-ISO' and the upcoming improved CAN FD controllers as
'ISO' compliant. See at http://www.can-cia.com/index.php?id=1937
Finally there will be three types of CAN FD controllers in the future:
1. ISO compliant (fixed)
2. non-ISO compliant (fixed, like the M_CAN IP v3.0.1 in m_can.c)
3. ISO/non-ISO CAN FD controllers (switchable, like the PEAK USB FD)
So the current M_CAN driver for the M_CAN IP v3.0.1 has to expose its non-ISO
implementation by setting the CAN_CTRLMODE_FD_NON_ISO ctrlmode at startup.
As this bit cannot be switched at configuration time CAN_CTRLMODE_FD_NON_ISO
must not be set in ctrlmode_supported of the current M_CAN driver.
Signed-off-by: Oliver Hartkopp <socketcan@hartkopp.net>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
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When changing flags in the CAN drivers ctrlmode the provided new content has to
be checked whether the bits are allowed to be changed. The bits that are to be
changed are given as a bitfield in cm->mask. Therefore checking against
cm->flags is wrong as the content can hold any kind of values.
The iproute2 tool sets the bits in cm->mask and cm->flags depending on the
detected command line options. To be robust against bogus user space
applications additionally sanitize the provided flags with the provided mask.
Cc: Wolfgang Grandegger <wg@grandegger.com>
Signed-off-by: Oliver Hartkopp <socketcan@hartkopp.net>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
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This patch completely removes the sync_with_hw() because it was broken and
actually there is no point of using it.
This function was used to:
- Make sure that the submitted packet to the HIQ (which is a kernel queue) was
read by the CP. However, it was discovered that the method this function used
to do that (checking wptr == rptr) is not consistent with how the actual CP
firmware works in all cases.
- Make sure that the queue is empty before issuing the next packet. To achieve
that, the function blocked amdkfd from continuing until the recently
submitted packet was consumed. However, the acquire_packet_buffer() already
checks if there is enough room for a new packet so calling sync_with_hw() is
redundant.
Signed-off-by: Oded Gabbay <oded.gabbay@amd.com>
Acked-by: Alex Deucher <alexander.deucher@amd.com>
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Signed-off-by: Oded Gabbay <oded.gabbay@amd.com>
Acked-by: Alex Deucher <alexander.deucher@amd.com>
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In order not to occupy the current core and thus prevent the core from
servicing IOMMU PPR requests, this patch replaces the call in DQM to
cpu_relax() with a call to schedule().
Signed-off-by: Oded Gabbay <oded.gabbay@amd.com>
Acked-by: Alex Deucher <alexander.deucher@amd.com>
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Other tunnels like GRE break while VxLAN offloads are enabled in Skyhawk-R. To
avoid this, we should restrict offload features on a per-packet basis in such
conditions.
Signed-off-by: Sriharsha Basavapatna <sriharsha.basavapatna@emulex.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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git://git.kernel.org/pub/scm/linux/kernel/git/rzhang/linux
Pull thermal fixes from Zhang Rui:
"Specifics:
- bogus type qualifier fix in OF thermal code.
- Minor fixes on imx and rcar thermal drivers.
- Update TI SoC thermal maintainer entry.
- Updated documentation of OF cpufreq cooling register"
* 'thermal-soc' of git://git.kernel.org/pub/scm/linux/kernel/git/rzhang/linux:
thermal: rcar: Spelling/grammar: s/drier use .../driver uses ...s/
thermal: rcar: change type of ctemp in rcar_thermal_update_temp()
thermal: rcar: fix ENR register value
Documentation: thermal: document of_cpufreq_cooling_register()
Thermal: imx: add clk disable/enable for suspend/resume
MAINTAINERS: update ti-soc-thermal status
MAINTAINERS: Add linux-omap to list of reviewers for TI Thermal
thermal: of: Remove bogus type qualifier for of_thermal_get_trip_points()
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It is useful to know at debug time if we are keeping main link on.
Signed-off-by: Rodrigo Vivi <rodrigo.vivi@intel.com>
Reviewed-by: Durgadoss R <durgadoss.r@intel.com>
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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No functional changes on this patch. Just grouping the link_standy decision
to avoid miss any change. Also making this info available everywhere
which will help to decide when to use vbt's tp time on following patch.
Signed-off-by: Rodrigo Vivi <rodrigo.vivi@intel.com>
Reviewed-by: Durgadoss R <durgadoss.r@intel.com>
[danvet: Slight editing of the commit message which was one huge
run-on sentence.]
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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Let's respect vbt full_link (link_standby) on source side as well.
Signed-off-by: Rodrigo Vivi <rodrigo.vivi@intel.com>
Reviewed-by: Durgadoss R <durgadoss.r@intel.com>
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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We have only two possible states with so many names and combinations that
might be confusing.
1 - Main link active / enabled / stand by / on
2 - Main link disabled / off / full off
Let's start organizing it by fixing a inverted logic when setting the sink bit.
Signed-off-by: Rodrigo Vivi <rodrigo.vivi@intel.com>
Reviewed-by: Durgadoss R <durgadoss.r@intel.com>
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
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